Cooper Energy Limited provide the following operations update. The average processing rate at the Orbost Gas Processing Plant (OGPP), owned and operated by APA Group, was 35 TJ/day in October and in line with the prior month. Average processing rates returned to 45 TJ/day on 30 October following cleaning of both sulphur absorbers during the last week of October. Following installation of new spray nozzles from late September to early October, OGPP produced at 45 TJ/day for most of a two-week period with the absorbers operating continually for more than three weeks. During the latest cleaning process, both spray nozzles were removed to allow for further assessment focused on optimizing solution dispersion to minimize foaming and improve H2S absorption. Re-installation of the spray nozzles is expected this quarter. Installation of the solids filtration system is on schedule for the March quarter. Long-lead items are arriving on site and preparations for installation are underway. The filtration system is the major component of the OGPP Phase 2B works, as announced on 19 August 2021. Sole gas sales volume: High demand has continued with sales into the Sole Gas Sales Agreements (GSAs) at maximum daily quantities. The average gas sales volume in October was 59 TJ/day, with OGPP processing shortfalls met through Cooper Energy's back-up gas supply arrangements and Otway Basin production. All daily nominations from Sole customers continue to be met. Sole gas field performance: The Sole gas field continues to perform in line with expectations.